Coupling Imbalance
Case History Number 5
It
all started with a 'phone call to the on-site office from a concerned PU Engineer, who
requested a vibration survey on one of the units large steam turbine driven Demag
compressors during commissioning back into service after a planned shutdown. The Engineer
had been informed that the Bently Nevada on-line condition monitoring system was
registering higher than previously experienced vibration levels on the turbine.
Historical data recorded on our on site database revealed that vibration levels prior to
the process unit shut down were normal for all bearing cap readings and also the Bently
Nevada displacement probe data. Bearing cap readings that day were typically below 2mm/sec
rms and gave no cause for concern. However, during start-up with the machine running at
7170 rpm, the Bently Nevada probes indicated the highest overall shaft vibration relative
to the bearings of about 32 microns. When the running speed was increased to 8500 rpm the
highest overall shaft displacement increased to over 43 microns see Figure 1 below.

Figure 1 - Trend plot
indicating overall vibration level changes.
Examination of the vibration
spectrum exhibited a dominant component at the running speed frequency with an amplitude
of 38 microns pk-pk indicating a probable imbalance condition of the turbine rotating
element. Further questioning revealed that a new rotating element had been fitted to the
turbine during the January 1995 shutdown, strongly suggesting the turbine as the source of
vibration, as levels on the compressor exhibited little change from previous tests. To
confirm this, the turbine was uncoupled from the compressor and run up to 7250 rpm with
the coupling boss still in place. The running speed component was now less than 10
microns, clearly the turbine rotor itself was not at fault and attention switched to the
coupling.
As this was the same coupling that was producing under 15 microns prior to the shutdown,
suspicion turned to the build up of the coupling and its associated packing pieces/shims.
During inspection of the coupling it was noticed that the spacers between the coupling
bosses and the spool piece had been fitted in a different configuration to that prior to
shutdown. The coupling was re-fitted according to all the match-marks and the coupled unit
was run up to 9000 rpm. Highest reading of around 10 microns clearly indicated that the
source of the imbalance had been correctly located and rectified. See Figures 2 and 3
below (before and after)

Figure 2 - Before
coupling correction

Figure 3 - After coupling
correction
The
process unit was brought on-stream 12 hours ahead of the planned schedule, generating
approximately £50,000.00 of extra production. Due to the prompt action in determining and
correcting the problem, thus preventing any secondary component damage such as a wiped
turbine drive end bearing, it is estimated that the cost savings due to this action
would be as follows :
assuming damage to the
turbine bearing had occurred,
time to
repair bearing 2-3 days lost production at : £50000.00/day
material
costs : £25000.00
Total
estimated savings : £175,000.00

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